RESEARCH ARTICLE

Industrial-scale investigations on effects of tertiary-air declination angle on combustion and steam temperature characteristics in a 350-MW supercritical down-fired boiler

  • Xiaoguang LI 1 ,
  • Lingyan ZENG , 1 ,
  • Hongye LIU 1 ,
  • Yao LI 2 ,
  • Yifu LI 2 ,
  • Yunlong ZHAO 3 ,
  • Bo JIAO 3 ,
  • Minhang SONG 1 ,
  • Shaofeng ZHANG 1 ,
  • Zhichao CHEN 1 ,
  • Zhengqi LI 1
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  • 1. School of Energy Science and Engineering, Harbin Institute of Technology, Harbin 150001, China
  • 2. Guizhou Wanfeng Electric Power Co., Ltd., Xingyi 562400, China
  • 3. Guizhou Xingyi Project Department, Huadian United (Beijing) Power Engineering Co., Ltd., Xingyi 562400, China

Received date: 17 Sep 2019

Accepted date: 15 Jan 2020

Published date: 15 Mar 2021

Copyright

2020 Higher Education Press

Abstract

Industrial-scale experiments were conducted to study the effects of tertiary air declination angle (TDA) on the coal combustion and steam temperature characteristics in the first 350-MW supercritical down-fired boiler in China with the multiple-injection and multiple-staging combustion (MIMSC) technology at medium and high loads. The experimental results indicated that as the TDA increased from 0° to 15°, the overall gas temperature in the lower furnace rose and the symmetry of temperature field was enhanced. The ignition distance of the fuel-rich coal/air flow decreased. In near-burner region, the concentration of O2 decreased while the concentrations of CO and NO increased. The concentration of NO decreased in near-tertiary-air region. The carbon in fly ash decreased significantly from 8.40% to 6.45% at a load of 260 MW. At a TDA of 15°, the ignition distances were the shortest (2.07 m and 1.73 m) at a load of 210 MW and 260 MW, respectively. The main and reheat steam temperatures were the highest (557.2°C and 559.4°C at a load of 210 MW, 558.4°C and 560.3°C at a load of 260 MW). The carbon in fly ash was the lowest (4.83%) at a load of 210 MW. On changing the TDA from 15° to 25°, the flame kernel was found to move downward and the main and reheat steam temperatures dropped obviously. The change of TDA has little effect on NOx emissions(660–681 mg/m3 at 6% O2). In comprehensive consideration of the pulverized coal combustion characteristics and the unit economic performance, an optimal TDA of 15° is recommended.

Cite this article

Xiaoguang LI , Lingyan ZENG , Hongye LIU , Yao LI , Yifu LI , Yunlong ZHAO , Bo JIAO , Minhang SONG , Shaofeng ZHANG , Zhichao CHEN , Zhengqi LI . Industrial-scale investigations on effects of tertiary-air declination angle on combustion and steam temperature characteristics in a 350-MW supercritical down-fired boiler[J]. Frontiers in Energy, 2021 , 15(1) : 132 -142 . DOI: 10.1007/s11708-020-0803-z

Acknowledgments

This work was supported by the National Natural Science Foundation of China (51706054) and the China Postdoctoral Science Foundation (Grant No. 2019M660633).
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